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01-03-2015, 11:35 PM | #133 |
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My belief is that the techs/robots assembling the engine at the factory followed the prescribed torque procedure, but that either that torque procedure and/or forces from high rpm use caused the rod bolts to be pushed past their yield point and they permanently stretched (lengthened) a small amount. Once they were in a permanently stretched state they lost some/most of their clamping force on the bearing. Lower clamping force on the bearing led to higher bearing wear and finally failure. This permanent stretching would also have led to a reduced measured torque value for the bolts on dis-assembly as Malek is reporting.
I'd be very interested to hear exactly what was measured in terms of reduced torque on 4 & 5. I just lost a motor in very similar circumstances to Malek's (2011, 43k, no mods) and this is the only explanation that makes any sense to me.
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01-04-2015, 07:17 AM | #134 |
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When did BMW go to doing the 3 stage torque sequence 3 times for new rod bolts? Did it start prior to the S65/85? I had not seen it specified for the S54 or S52. but have not seen everything. If it came out sometime recently, maybe it is an indication BMW knew there were issues with new rod bolts. I did the 3 stages 3 times for each bolt when I changed bearings and bolts this summer and thought it was a pain in the rear and was wondering why it was necessary. Seemed like I was pre-stretching the bolts.
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01-04-2015, 07:55 AM | #135 |
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Malek, in your own personal situation, what ultimately will happen to the engine? Can it be repaired or is it toast? We now know this is an issue, I'm just curious how often engines can be repaired after failure and at what cost.
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01-04-2015, 12:19 PM | #136 | |
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01-04-2015, 12:31 PM | #137 | |
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01-04-2015, 12:32 PM | #138 | |
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01-04-2015, 12:34 PM | #139 | |
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01-04-2015, 01:59 PM | #140 |
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Will explain more later but there are no signs of the bolts being loose.
Look at the bearing wiki and I posted pictures of bearings that are moving around in the saddle from bolts that are not good enough or too little crush. The back side of many bearings do not show they have been moving in the saddle. It cant happen folks. If the stretch is lost the bolt will fall out. I have yet to see a bearing that is moving in the saddle of the rod and yet to see a rod that is fretted at the parting line. Have many experiences with bolts that are inadequate even with doweled rods. If the bolts do not have enough clamp load it will shear the dowel pins in half. Have seen this happen on many occasions. There is no evidence that the broken caps are fretting together. Also, it is impossible to measure break away torque on a TTY bolt. One cannot say a bolt was loose from factory if it is a TTY bolt Can the s65 benefit from the better bolts... of course, bolts cant come loose and continue to run. If there were enough force to stretch the bolt beyond its original state and lose clamp load the bolt will eventually come out because every time it stretched it becomes looser and looser.
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01-04-2015, 02:21 PM | #141 | |
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01-04-2015, 03:07 PM | #142 |
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I assume he would say inadequate clearances. It's a good theory but doesn't explain Malek's finding with the VAC bearings. VAC and Harrop are not idiots and they employ thicker bearings apparently with some success. This suggests the clearances theory is not a 100% lock (or that there are other factors at play in addition to clearances).
Last edited by Hujan; 01-25-2015 at 02:38 PM.. |
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01-04-2015, 03:17 PM | #143 | |
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01-04-2015, 04:26 PM | #144 |
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When I looked up the S54 torque, I saw just one 3 stage sequence. No requirement it be repeated 3 times for new bolts. No big deal doing a 3 stage versus the arp single stage, but it is a pain to do a 3 stage 3 times for each bolt.
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01-04-2015, 06:17 PM | #145 | |
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I have been asked many times how one can measure bolt torque on the BMW stretch hardware (Torque to Yield), definitively you cannot, this is an obvious fact. However, a crude way of checking it is still possible in the hands of the assembler, and I am sure you know this better than many as this is what you do for a living. With the Snap-On Tech-Angle torque wrenches, when set in reverse, one can simply observe how many degrees it takes while releasing the fastener until it breaks loose. Cylinders 5+6 on my own engine with respect to connecting rod bolts broke free much sooner and easier than the other connecting rods. Please don't take this that my findings definitively indicate the hardware being the end all problem and that upgraded hardware is the solution. Interestingly enough, no thoughts have expressed any on how the bearings from the first engine posted are BETTER with the Calico coated bearings (which have been known to be worse for bearing clearances, with ARP hardware after 33,xxx miles vs. the OE bearings + OE hardware from the same engine with the same rods and same crankshaft at 6000 miles. Things we know 100% from the first engine: -Same crankshaft -Same connecting rods -First 6000 miles used with OE Bearings+Bolts show excessive and worrisome bearing wear. -Remaining 33,xxx miles are on Calico coated OE bearings+ ARP rod bolts showing no bearing wear. Things that will be done with first engine: -Crankshaft will be mic'd for specifications on all 8 journals. -Connecting rod clearances calculated with rods loaded with the original OE bearings and torqued with OE hardware. -Bearing shell thickness will be mic'd for both Calico coated bearings and the OE bearing shells. The point of this thread wasn't to engage in some sort of contest as to who is right and who is wrong; the point is to share information. I am not sure why this thread is being sidetracked into anything else but that. Please see above. I will take the time to spec these engines out. It's the only way to be sure of anything.
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01-04-2015, 06:34 PM | #146 | |
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01-04-2015, 06:42 PM | #147 | |
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At this point the only thing that can be re-used from the original engine are the accessories and the cylinder heads and associated parts not related to the block and rotating assembly. Cylinder 1+2 have some scratching on the cylinder walls as well as cylinders 5+6. The Pistons themselves on those corresponding cylinders have some scratching on them as well. If pictures are wanted to depict the damage more clearly, I can post those as well tomorrow when I am back at the shop.
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01-04-2015, 08:31 PM | #148 |
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Wow, nasty stuff.
Malek, if this car was stock other than exhaust, and only has 39k miles, isn't it still under warranty, if so could you get bmw to do the right thing and pay for a new motor? I know you are tearing it down for the sake of research and sharing info, but it sucks that you have to eat the cost of a motor because of that.
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01-04-2015, 09:00 PM | #149 |
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01-04-2015, 09:08 PM | #150 | |
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The same engine that showed severe bearing wear at 6,000 miles with OEM bearings and bolts, magically showed no wear after 30,000 with VAC coated bearings (i.e., thicker than OEM bearings) and ARP bolts. Unless the clearances magically got significantly looser after 6,000 miles, you have to admit this is a bit of a head-scratcher if the root cause of the initial bearing wear was excessively tight clearances. The only variable between the two was a supercharger. Do you believe that actually helps ameliorate tight rod-bearing clearances? If so, I would appreciate understanding the physics involved. |
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01-05-2015, 02:34 AM | #151 | |
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01-05-2015, 10:52 AM | #153 | |
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Don't sweat it Malek, I take your word for it. Sounds like you are busy enough big guy!
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01-05-2015, 10:20 PM | #154 | |
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